Teardown and Repair of a Galaxy's Edge C1-10P Droid

My C1-10P droid from Galaxy's Edge has always had an issue with its head. Whenever reacting to a beacon the head would turn all the way to its left and then get stuck there when it should normally turn back to its right. In this video I take apart my droid to try and solve the problem with Chopper's head which includes using an undocumented debug mode that is built into all Galaxy's Edge droids to verify the issue and whether or not the repair worked. If you're interested in the motion activate bluetooth beacon I use in this video see this video where I demonstrate it:    • A Motion Activated Droid   and this shared project on OSHPark where you can order copies of the PCB for yourself: https://oshpark.com/shared_projects/q... 0:00 Introducing the Droid Debug Mode 2:42 Debugging Chopper 4:30 Disassembling Chopper 12:01 Head Position Detection Mechanism 13:29 Cleaning The Tracks 17:05 Reassembly 26:42 Testing and Conclusion